World literature has introduced the aerodynamic importance of unsteadiness in turbines. In particular, the unsteady static pressure field determines the work of the machine. The unsteadiness can redistribute the total pressure in a cascade with wake interaction. It has been shown that differences in work between wake and free stream can act to rectify the wakes and boost efficiency. In this paper, fast response aerodynamic probe (FRAP) data are used to study the nature of the unsteady work in the flow at entry to and exit from a rotating turbine blade. The topic is addressed experimentally, theoretically, and computationally. It is found at both rotor inlet and exit that upstream wakes influence the unsteady work distribution. The relationship between the unsteady work in the absolute frame, the relative frame, and the momentum of the fluid circumferentially is derived and verified experimentally. Computational results (unsteady Reynolds-averaged Navier–Stokes (URANS)) are compared to the experimental results: reasonable agreement is found at rotor exit, but significant differences at rotor inlet are found. The computational fluid dynamics (CFD) has failed to capture the von Karman vortices and has dramatically lower levels of unsteady work. The experimental unsteady work distribution suggests possible effects of wake bending and vortex instability.
Skip Nav Destination
Article navigation
November 2013
Research-Article
Experimentally Observed Unsteady Work at Inlet to and Exit From an Axial Flow Turbine Rotor
Philipp Jenny,
Philipp Jenny
LEC-ETHZ
,Zurich
CH-8092, Switzerland
Search for other works by this author on:
Jochen Gier,
Jochen Gier
MTU Aero Engines
,Munchen D-80995
, Germany
Search for other works by this author on:
Reza S. Abhari
Reza S. Abhari
LEC-ETHZ
,Zurich CH-8092
, Switzerland
Search for other works by this author on:
Martin G. Rose
Philipp Jenny
LEC-ETHZ
,Zurich
CH-8092, Switzerland
Jochen Gier
MTU Aero Engines
,Munchen D-80995
, Germany
Reza S. Abhari
LEC-ETHZ
,Zurich CH-8092
, Switzerland
Contributed by the International Gas Turbine Institute of ASME for publication in the JOURNAL OF TURBOMACHINERY. Manuscript received June 29, 2012; final manuscript received December 11, 2012; published online September 13, 2013. Editor: David Wisler.
J. Turbomach. Nov 2013, 135(6): 061017 (8 pages)
Published Online: September 13, 2013
Article history
Received:
June 29, 2012
Revision Received:
December 11, 2012
Citation
Rose, M. G., Jenny, P., Gier, J., and Abhari, R. S. (September 13, 2013). "Experimentally Observed Unsteady Work at Inlet to and Exit From an Axial Flow Turbine Rotor." ASME. J. Turbomach. November 2013; 135(6): 061017. https://doi.org/10.1115/1.4023460
Download citation file:
Get Email Alerts
Cited By
Related Articles
The Effect of Unequal Admission on the Performance and Loss Generation in a Double-Entry Turbocharger Turbine
J. Turbomach (March,2012)
Design Principles and Measured Performance of Multistage Radial Flow Microturbomachinery at Low Reynolds Numbers
J. Fluids Eng (November,2008)
A Comparison of the Flow Structures and Losses Within Vaned and Vaneless Stators for Radial Turbines
J. Turbomach (July,2009)
Related Chapters
Outlook
Closed-Cycle Gas Turbines: Operating Experience and Future Potential
Performance and Mechanical Equipment Standards
Handbook for Cogeneration and Combined Cycle Power Plants, Second Edition
Introduction
Turbine Aerodynamics: Axial-Flow and Radial-Flow Turbine Design and Analysis